Start-Up Evaluation of a Full-Scale Wastewater Treatment Plant Consisting of a UASB Reactor Followed by Activated Sludge

dc.contributor.authorDíaz Gómez, Jaime
dc.contributor.authorPérez Vidal, Andrea
dc.contributor.authorVargas Nuncira, David
dc.contributor.authorUsaquén Perilla, Olga
dc.contributor.authorJiménez Daza, Ximena
dc.contributor.authorRodríguez, Claudia
dc.date.accessioned2025-03-28T22:21:24Z
dc.date.available2025-03-28T22:21:24Z
dc.date.issued2022-12
dc.description.abstractUASB (upflow anaerobic sludge blanket) reactors have been recognized as a viable option for sewage treatment. However, in order to improve the UASB effluent quality, some type of post-treatment must be implemented. The aims of this study were (i) to establish a start-up methodology of a full-scale anaerobic–aerobic system treating sewage, (ii) to evaluate the concentrations of different constituents in the influent and effluent of the anaerobic and aerobic reactors as well as the removal efficiencies in every step of the system, and (iii) to define relevant operative aspects of the anaerobic and aerobic reactors. The Tunja (Colombia) wastewater treatment plant consists of three modules with preliminary treatment followed by UASB reactors with post-treatment of activated sludge. The results of this investigation showed that the effluent system meets the Colombian environmental legislation with average removal efficiency values of BOD (88 +/− 5%), COD (87 +/− 4%), and TSS (94 +/− 5%). The UASB reactor start-up was conducted without an inoculum, requiring a period of 120 days. The evaluation of the combined systems was conducted over 300 days. Moreover, a methodology to operate the system during and after the start-up of the anaerobic reactor was defined. It was demonstrated that the anaerobic effluent can deteriorate the sludge in the aerobic tank. In order to avoid this, important operational aspects must be considered during the operation of the system, such as the implementation of a raw wastewater bypass higher than 15% and monitoring of the anaerobic effluent settleable solid concentration (<0.3 mL/L).
dc.identifier.citationDíaz-Gómez, J., Pérez-Vidal, A., Vargas-Nuncira, D., Usaquén-Perilla, O., Jiménez-Daza, X., & Rodríguez, C. (2022). Start-Up Evaluation of a Full-Scale Wastewater Treatment Plant Consisting of a UASB Reactor Followed by Activated Sludge. Water (Switzerland), 14(24). https://doi.org/10.3390/w14244034
dc.identifier.issn20734441
dc.identifier.urihttps://repositorio.usc.edu.co/handle/20.500.12421/6144
dc.language.isoen
dc.subjectanaerobic treatment
dc.subjectaerobic treatment
dc.subjectUASB
dc.subjectactivated sludge
dc.subjectpost-treatment
dc.titleStart-Up Evaluation of a Full-Scale Wastewater Treatment Plant Consisting of a UASB Reactor Followed by Activated Sludge
dc.typeArticle

Files

Original bundle
Now showing 1 - 1 of 1
No Thumbnail Available
Name:
Start-Up Evaluation of a Full-Scale Wastewater Treatment Plant Consisting of a UASB Reactor Followed by Activated Sludge.pdf
Size:
3.11 MB
Format:
Adobe Portable Document Format
License bundle
Now showing 1 - 1 of 1
No Thumbnail Available
Name:
license.txt
Size:
1.71 KB
Format:
Item-specific license agreed upon to submission
Description: