Repository logo
  • English
  • Español
  • Log In
    New user? Click here to register. Have you forgotten your password?
Repository logo
  • Communities & Collections
  • All
  • English
  • Español
  • Log In
    New user? Click here to register. Have you forgotten your password?
  1. Home
  2. Browse by Author

Browsing by Author "Vargas Nuncira, David"

Now showing 1 - 1 of 1
Results Per Page
Sort Options
  • No Thumbnail Available
    Item
    Start-Up Evaluation of a Full-Scale Wastewater Treatment Plant Consisting of a UASB Reactor Followed by Activated Sludge
    (2022-12) Díaz Gómez, Jaime; Pérez Vidal, Andrea; Vargas Nuncira, David; Usaquén Perilla, Olga; Jiménez Daza, Ximena; Rodríguez, Claudia
    UASB (upflow anaerobic sludge blanket) reactors have been recognized as a viable option for sewage treatment. However, in order to improve the UASB effluent quality, some type of post-treatment must be implemented. The aims of this study were (i) to establish a start-up methodology of a full-scale anaerobic–aerobic system treating sewage, (ii) to evaluate the concentrations of different constituents in the influent and effluent of the anaerobic and aerobic reactors as well as the removal efficiencies in every step of the system, and (iii) to define relevant operative aspects of the anaerobic and aerobic reactors. The Tunja (Colombia) wastewater treatment plant consists of three modules with preliminary treatment followed by UASB reactors with post-treatment of activated sludge. The results of this investigation showed that the effluent system meets the Colombian environmental legislation with average removal efficiency values of BOD (88 +/− 5%), COD (87 +/− 4%), and TSS (94 +/− 5%). The UASB reactor start-up was conducted without an inoculum, requiring a period of 120 days. The evaluation of the combined systems was conducted over 300 days. Moreover, a methodology to operate the system during and after the start-up of the anaerobic reactor was defined. It was demonstrated that the anaerobic effluent can deteriorate the sludge in the aerobic tank. In order to avoid this, important operational aspects must be considered during the operation of the system, such as the implementation of a raw wastewater bypass higher than 15% and monitoring of the anaerobic effluent settleable solid concentration (<0.3 mL/L).

Higher Education Institution subject to inspection and surveillance by the Ministry of National Education.
Legal status granted by the Ministry of Justice through Resolution No. 2,800 of September 2, 1959.
Recognized as a University by Decree No. 1297 of 1964 issued by the Ministry of National Education.

Institutionally Accredited in High Quality through Resolution No. 018144 of September 27, 2021, issued by the Ministry of National Education.

Ciudadela Pampalinda

Calle 5 # 62-00 Barrio Pampalinda
PBX: +57 (602) 518 3000
Santiago de Cali, Valle del Cauca
Colombia

Headquarters Centro

Carrera 8 # 8-17 Barrio Santa Rosa
PBX: +57 (602) 518 3000
Santiago de Cali, Valle del Cauca
Colombia

Palmira Section

Carrera 29 # 38-47 Barrio Alfonso López
PBX: +57 (602) 284 4006
Palmira, Valle del Cauca
Colombia

DSpace software copyright © 2002-2025 LYRASIS

  • Cookie settings
  • Privacy policy
  • End User Agreement
  • Send Feedback

Hosting & Support